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Thread: Great News!!!!!!

  1. #21
    Member Graham's Avatar
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    Quote Originally Posted by Dan View Post
    just make sure you bore a scope the hole first It sounds like a piston issue.
    Good luck


    if you need to borrow a bore a scope we have one we will lend you to verify the problem before you take it apart
    Thanks for the offer! If we do end up needing that I'll let you know

  2. #22
    Senior Member jjmatheson's Avatar
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    That is bad, Im sorry for your experience. That is why I would not run fourteen p.s.i. on a stock Eaton, especially with 91 octane. Why did they not take timing out on the first run then add timing on the following runs. More boost is not always better, spinning the blower faster means more heat. Save your money and buy a Whipple.

  3. #23
    Senior Member ASUSMC's Avatar
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    It didn't have any timing in it. The first 3 runs were made with 10 degrees total timing. That and I am pretty sure the blower is ported. Has to be a home port its just too loud to not be ported and I don't see any Steig stamps or numbers anywhere. I will find out when it comes off. Probably could use a rebuild. First things first find out how bad the motor is and decide what I am going to do about it.

    For the record I am not blaming Keith or Arizona Dyno chip for any of this.
    2012 Race Red GT w/ a 5 Liter and a 6 speed
    2010 Dodge Challenger R/T traded in.
    '03 DBS Cobra .... Traded in, THANK GOD
    '01 Ford Lightning.... Sold, sorely missed

  4. #24
    Member Graham's Avatar
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    Quote Originally Posted by jjmatheson View Post
    That is bad, Im sorry for your experience. That is why I would not run fourteen p.s.i. on a stock Eaton, especially with 91 octane. Why did they not take timing out on the first run then add timing on the following runs. More boost is not always better, spinning the blower faster means more heat. Save your money and buy a Whipple.
    Its not a stock eaton

  5. #25
    Senior Member Ethan@S3M's Avatar
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    Quote Originally Posted by ASUSMC View Post
    It didn't have any timing in it. The first 3 runs were made with 10 degrees total timing. That and I am pretty sure the blower is ported. Has to be a home port its just too loud to not be ported and I don't see any Steig stamps or numbers anywhere. I will find out when it comes off. Probably could use a rebuild. First things first find out how bad the motor is and decide what I am going to do about it.

    For the record I am not blaming Keith or Arizona Dyno chip for any of this.
    Its has more to do with the oil consumption than the dyno or tuner.

  6. #26
    Senior Member jjmatheson's Avatar
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    Well good luck

  7. #27
    Senior Member WildBill's Avatar
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    Quote Originally Posted by Graham View Post
    It's better to pull the injector instead. If you pull the cop It will keep dumping fuel...no bueno
    How many miles ya gonna drive it? LOL! ....10 seconds ain't gonna hurt. ;)

  8. #28
    Administrator BurnTire's Avatar
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    Quote Originally Posted by Ethan@S3M View Post
    This will fix it!!!!!

    Whats that a Devin Bottle Rocket
    Sold
    2004 Cobra, Whipple ,TH-400
    Burning Corn
    9.97 - 135.5

  9. #29
    Senior Member AZSonicSnake's Avatar
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    Quote Originally Posted by Ethan@S3M View Post
    Its has more to do with the oil consumption than the dyno or tuner.
    so i have to ask the question, how would the tuner not pick this out before making so many pulls? seems to me like that would be something easy to spot...

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  10. #30
    Senior Member ASUSMC's Avatar
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    Can't really spot oil pushing through the pcv system. The truck doesn't have an oil separator on it yet so you are not going to see it. Its not Keiths fault regardless. He has hundreds if not thousands of cars on the road and is a VERY well respected tuner. Sometimes shit just happens.
    2012 Race Red GT w/ a 5 Liter and a 6 speed
    2010 Dodge Challenger R/T traded in.
    '03 DBS Cobra .... Traded in, THANK GOD
    '01 Ford Lightning.... Sold, sorely missed

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