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Thread: nitrous + track =..

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  1. #1
    Senior Member Ruckus46gt's Avatar
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    nitrous + track =..

    issues..Had issue nitrous cutting out, it would spray 2nd and then cut out and stay off. It also wouldnt spray out of the hole. I have no idea if my fpss was cutting the nitrous off, if the interface controller was, or what but i'm not happy. Spraying the one gear here is the slip
    60'.....1.832
    330....5.034
    1/8....7.772
    mph...89.005
    1000..10.097
    1/4....12.189
    mph...111.382
    i have no idea whats going on have a week to figure it out

  2. #2
    Senior Member wickedcobra's Avatar
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    Gold Award 
    Nothing worse than all that anticipation and crap doesn't work.

  3. #3
    Senior Member Ruckus46gt's Avatar
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    think i might have fixed the issue either that or for some reason i just stalled it up on the street went full throttle and as soon as it flashed to 3k the nitrous kicked in and stayed in through all the gear. only thing i did was move a ground, before the switch panel ground and window switch ground were the same. i'm debating on going back to the track tonight but dont think thats the issue. what do you think worked fine on the dyno...but then again thats one gear only

  4. #4
    Senior Member Ruckus46gt's Avatar
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    same issue tonight except got the car to spray out of the hole, but didnt spray up to 12.10@111.4 i ran

  5. #5
    Senior Member Ruckus46gt's Avatar
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    think i found out the issue turns out the interface jet portion is only supposed to be used when doing doing a dry shot (instructions dont say either), so in reality i was hitting the car with a 100 shot of nitrous and a 175 shot of fuel. That explains how rich the car was etc, so looks like i'll be heading back to a dyno to check the af with just the pill interface set to 0 and see if that was the issue. Might have been almost blowing out the spark up top and thats why it didnt respond past the inital hit

  6. #6
    Senior Member 93mustank's Avatar
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    Glad it was an easy fix.... Cant wait to see what it runs with a working 100 shot ....should go 11.6's

  7. #7
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    mine was doing the same thing last year...it sprayed on the dyno (100 shot) and I went to the track...spray it and no gains at all. go on the street...nothing. I added a tach adapter because the Mod motors toss out an irregular signal (some use them, some dont) and went on the street and it worked....trying to get to the track march/april
    Jake
    Silver '03 Cobra Coupe Auto
    9.82 @ 135 w/ a 1.35 - NO Nitrous!

    9.50 @ 139 w/ a 1.30 - Nitrous

    **Click here for all my video's!!!**


  8. #8
    Senior Member Ruckus46gt's Avatar
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    i took off another safety device yesterday so hopefully it should work now. I noticed at the track yesterday that it did show 111 but the bottle had some weight to it still approx 3lbs left in it but no nitrous left just air so didnt get a good run in after the initial hit it jsut fell off again. Hopefully all is good with the system...event this weekend. I have the tach signal set up right for (4 cylinder...thats how its supposed to be set up according to the company and where i tapped it)

  9. #9
    The Nunn's
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    Quote Originally Posted by Ruckus46gt View Post
    i took off another safety device yesterday so hopefully it should work now. I noticed at the track yesterday that it did show 111 but the bottle had some weight to it still approx 3lbs left in it but no nitrous left just air so didnt get a good run in after the initial hit it jsut fell off again. Hopefully all is good with the system...event this weekend. I have the tach signal set up right for (4 cylinder...thats how its supposed to be set up according to the company and where i tapped it)
    when the bottle is at 3# or lower you dont have the adequate amount of nitrous to have the correct pressure throughout the run. a good rule of thumb is 2# per 100 shot so you'll get 4 good runs and on the 5th pass, performance will drop.

  10. #10
    Senior Member Ruckus46gt's Avatar
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    Quote Originally Posted by 2ND2NUNN View Post
    when the bottle is at 3# or lower you dont have the adequate amount of nitrous to have the correct pressure throughout the run. a good rule of thumb is 2# per 100 shot so you'll get 4 good runs and on the 5th pass, performance will drop.
    yea thats why i filled both bottles today for this weekend. I think something is up with my bottle though. I contacted the company today waiting for a response back. Hopefully they take care of me, i think there is a crack in the siphon tube or something since you heard it fizzing and it sounded like an orca whale the hole time

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