Well what I have feared most has now come true. After 3 weeks of working all day then staying until 3-4am every morning then returning to work at 9am and having the expense of rushing to get a enclosed trailer to make this trip (to the Storman Norman event) we have suffered a catastrophic loss. We fired the motor up Saturday morning and it sounded great so we went home. Later on that day we ran the motor once again to allow it to reach to operating tempter and then we heard it…….. A light faint Knock! The warmer the motor was the louder it became we acted quickly and found out that it was from the top end. Yes it is something from inside the valve cover it was something in the head that is making noise. Un fortunately in order to pull the intake you must take the front of the motor apart and if you add the time to pull the front apart and then the intake just to inspect what the noise is from will take so much time that we regrettably will not be able to make the trip, our window of time has now passed. So after caging the car working 20 hours a day for 3 weeks and driving to the end of the earth to get the proper trailer, and all the BS money that I have spent to make this happen it will regrettably not happen. So cross you fingers that I can get it apart and make the club day. I’m so pissed that I kicked the jack and now have broken my foot to boot! Anyone have suggestions?? I’m at a loss of words here